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1 | Reference No. | Date of Event | Brand/Vessel | Event Description | CAM Incident Category | Location | Violation | Substance | Quantity | Temp Mins | Type | ||||||||||||||
2 | 03-2017.1 | 9/1/2015 | HAL - Various Vessels | Between September 2015 and October 2016, vessel discharges in contravention of NOAA's marine sanctuary regulations were identified on 4 PCL ships and 1 HAL ship. Discharges were within the expanded boundaries of the Greater Farallones National Marine Sanctuary. Discharges were food waste, processed permeate, untreated grey water, membrane bioreactor sludge (not oil), advanced wastewater treatment system permeate, exhaust gas cleaning system ("EGCS") wash water, and treated sewage. | EGCS Voyage Planning | Greater Farallones National Marine Sanctuary waters | TRUE | Food waste, processed permeate, untreated grey water, membrane bioreactor sludge, advanced wastewater treatment system permeate, EGCS wash water and treated sewage | 13_months | Dumping | |||||||||||||||
3 | 03-2017.2 | 9/18/2016 | PCL Grand Princess | On December 2, 2016, while making preparations for the Grand Princess' voyage, the EO and the Voyage Planning Officer held a voyage planning meeting. During this meeting it was discovered that an "Environmental Limit Marker" on the planned track, similar to ones used for the 4 NM and 12 NM limits, was within the boundaries of the Cordell Bank National Marine Sanctuary. There were no "Environmental Limit Markers" around the boundaries of the expanded Cordell Bank and Greater Farallones Marine Sanctuaries. This discovery led to an investigation into whether the "Environmental Limit Marker" had been used during the 2016 summer season when the ship was sailing between San Francisco and Alaska. The initial internal investigation, conducted by the EO, confirmed that the ship had been discharging various waste streams as detailed in Annex 1 between May 11, 2016, and September 18, 2016, within the expanded boundaries of the Greater Farallones National Marine Sanctuary. | Not Applicable | Greater Farallones National Marine Sanctuary waters | TRUE | Various waste streams | 5_months | Dumping | |||||||||||||||
4 | 013_2017-FA | 11/7/2016 | Carnival Fantasy | 1,620 kg of refrigerant gas leaked from the ship's refrigeration systems in November 2016. Due to the lack of communication and awareness of record keeping, entries were not made in the refrigerant or oil record books. The missing entries have been added to the Refrigeration Record Book, incident reports have been completed, and the Oil Record Book was updated. | Oil Record Book Recordkeeping Refrigerants | FALSE | refrigerant gas | 1620_kg | Refrigerant | ||||||||||||||||
5 | CAM-00313 | 2/9/2017 | PCL Emerald Princess | Shore side was informed that on November 29, 2017, Maritime New Zealand filed criminal charges against PCL for two alleged violations of New Zealand’s Maritime Transport Act 1994 in connection with a fatal accident on board the Emerald Princess while docked in Port Chalmers, New Zealand on or about February 9, 2017. A high-pressure nitrogen cylinder burst while being re- pressurized, which resulted in the death of an Emerald Princess crew member standing nearby. The Transport Accident Investigation Commission (TAIC) in New Zealand investigated the incident and issued an interim report on May 10, 2017, concluding that the burst nitrogen cylinder had suffered significant corrosion at the point of failure. A metallurgist’s initial assessment also concluded that the failure had occurred as a result of overload caused by corrosion thinning. | Not Applicable | TRUE | Missing/Broken Parts | ||||||||||||||||||
6 | 01-17 | 4/9/2017 | Costa Deliziosa | On April 9, 2017, two Italian Coast Guard Petty Officers boarded the vessel for routine collection of MARPOL marine gas samples. The MARPOL samples of marine gas oil bunkered in Port Everglades on March 18, 2017, could not be found onboard, despite their recordation in the corresponding Bunker Delivery Note. This violated MARPOL Annex VI, Regulation 18.3.8.1 | Not Applicable | TRUE | Missing Records | ||||||||||||||||||
7 | 08-2017.1 | 4/19/2017 | AIDAluna | The ORB was not signed by an EO from April 19, 2017, to May 5, 2017, and from June 27, 2017, through August 18, 2017. Both the Captain and the Chief Engineer continued to sign each page during this period. There was an EO handover during this period, which may have been a contributing factor. The departing EO explained that he forgot to sign the completed ORB pages the referenced time periods. The boarding EO expected further clarification of the significance of her signature, so she did not sign the completed ORB pages from July 11, 2017 to August 18, 2017. The AIDA Environmental Manager was onboard at the time the issue was discovered. He discussed it with the current EO, who then signed all completed ORB pages from July 11, 2017, to August 18, 2017. The prior EO visited the ship on August 19, 2017, to sign the completed ORB pages and did so for those from June 27, 2017, to July 11, 2017, but forgot to sign the pages from April 19, 2017 to May 5, 2017. Shore side management was informed and arranged for the ORB pages from April 19, 2017, to May 5, 2017, to be signed. | Recordkeeping Oil Record Book | FALSE | Missing Records | ||||||||||||||||||
8 | CAM-00071 | 4/24/2017 | Carnival Triumph | The ORB had a missing entry for maintenance of the OCM performed on April 24, 2017. An 'I' entry was made in the ORB indicating the missing maintenance operation and the Captain, Chief Engineer, OLCM, and Director of Environmental Operations were informed. | Oil Record Book Recordkeeping | FALSE | |||||||||||||||||||
9 | CAM-00106 | 4/25/2017 | Carnival Ecstasy | During a review of the ORB, it was identified that a BCDB OCM cleaning operation was recorded in the PMS system but not in the ORB. The OLCM and shore side management were notified. | Recordkeeping | FALSE | Missing Records | ||||||||||||||||||
10 | CAM-00015 | 5/1/2017 | PCL Sea Princess | Ship discharged Ballast water early May while alongside in Hawaii without use of the installed Ballast Water Treatment System. The request to do so was made by the Staff Captain. Ballast water was initially treated on the way into the ship through the Hyde Guardian BWT system, but also needed to be treated on the way out, which it was not. | Voyage Planning | Hawaii port | FALSE | Dumping | |||||||||||||||||
11 | ECP 17-07-02 | 5/1/2017 | PCL Sun Princess | The EO sent an email to the HR department, with a copy to technical operations, providing notification that the Chief Engineer discovered that the solenoid valve on one of the OWS had been replaced with piping. The Chief Engineer noticed the missing solenoid valve sitting next to the OWS, and he replaced the piping with the valve. Based on AMOS maintenance records, the Chief Engineer believes that he identified the Engineer that implemented the piping. AMOS records indicate that the solenoid valve was due to be cleaned on routine basis (monthly), and the most recent AMOS record for such maintenance indicated that the cleaning had recently been performed/completed by the engineer in question. The engineer, however, went on leave two days prior to the Chief Engineer’s discovery of the piping. The HAG Safety Env. and Regulatory Services (SERS) group – Paul McClelland (the OLCM) and Kelly Clark (Senior VP) – received word of the issue via the technical operations group. SERS directed Jeanne Grasso (Blank Rome) to fly to Australia and board the ship on June 29, conduct an investigation into the issue, and disembark on July 1. | OWS/Whitebox | FALSE | Missing/Broken Parts | ||||||||||||||||||
12 | CAM-00016 | 5/8/2017 | Carnival Ecstasy | The Carnival Ecstasy was alongside port of Charleston operating on Heavy Fuel Oil for a number of hours without use of the EGCS. It appears the EGCS tripped out earlier in the day. It is unclear if the system failed to alarm upon trip or if the watch-keeper failed to respond. | EGCS | Charleston, South Carolina port | TRUE | HFO | EGCS | ||||||||||||||||
13 | CAM-00003 | 5/9/2017 | Carnival Glory | 156 kg of refrigerant gas leaked from a line connected to a provision system due to deteriorating materials and ship vibration. The line was repaired and system was put back in place. | Refrigerants | FALSE | refrigerant gas | 156_kg | Refrigerant | ||||||||||||||||
14 | CAM-00004 | 5/9/2017 | Carnival Inspiration | 102 kg of refrigerant gas leaked from an air conditioning compressor due to a cracked gasket. The gasket was replaced and the system was put back in service. | Refrigerants | FALSE | refrigerant gas | 102_kg | Refrigerant | ||||||||||||||||
15 | CAM-00005 | 5/9/2017 | P&O Azura | A sample pump on the EGCS stopped working but the system did not alarm or indicate a fault on the control panel. The pump was reset and no further issues have been reported. | EGCS | FALSE | Missing/Broken Parts | ||||||||||||||||||
16 | CAM-00424 | 5/9/2017 | PCL Star Princess | On May 15 and 16, 2017, PCL self-reported two separate test results of samples taken from the Star Princess on May 9, 2017, which indicated that the vessel's Biological Oxygen Demand ("BOD") levels exceeded the daily maximum allowed. PCL had the vessel's Membrane Bioreactors (the "MBR") inspected and discovered that blown gaskets created air leaks that caused the devices to become insufficiently aerated. To rectify the problem, PCL cleaned and sanitized the tanks, serviced the system, increased aeration in the buffer tank, added an additional 0.5 liters of Heeburn Bio ET to each jet, and revised the MBRs' desludging frequencies. On July 13, 2017, PCL received a Notice in response to these self-reported violations, plus three additional violations regarding daily and monthly BOD exceedances. | Not Applicable | TRUE | Missing/Broken Parts | ||||||||||||||||||
17 | CAM-00006 | 5/10/2017 | Carnival Elation | While underway, approximately 15 liters of MGO leaked overboard from a lifeboat due to a corroded fuel tank. The drain was plugged and the excess MGO was contained. The incident was also recorded as a Potentially Significant LSA Failure. | Lifeboat/Tender | FALSE | MGO | 15_liters | Dumping | ||||||||||||||||
18 | CAM-00007 | 5/10/2017 | HAL Eurodam | While alongside in Ketchikan, Alaska, a grey sheen was observed in the water on the starboard side of the area of the EGCS overboard discharge. A blocked filter was found to be the cause of the contamination. | EGCS | Ketchikan, Alaska port | FALSE | Sheen | Dumping | ||||||||||||||||
19 | CAM-00011 | 5/13/2017 | Cunard Queen Mary 2 | A pressure transducer on the forward OWS failed. The sensor was replaced and the OWS returned to service. | OWS/Whitebox | FALSE | Missing/Broken Parts | ||||||||||||||||||
20 | CAM-00010 | 5/13/2017 | HAL Westerdam | The BCDB (whitebox) data recorder has an intermittent fault resulting in lapses of data recording. An investigation is ongoing. | Not Applicable | FALSE | Missing/Broken Parts | ||||||||||||||||||
21 | CAM-00009 | 5/15/2017 | Costa Luminosa | The BCDB (whitebox) was taken out of service due to a data recorder failure. An urgent external service was arranged to determine the root cause of the failure and the necessary corrective actions. | Not Applicable | FALSE | |||||||||||||||||||
22 | CAM-00012 | 5/15/2017 | HAL Veendam | 2 pH sensors on the EGCS systems failed their calibration tests resulting in higher consumption of MGO. | EGCS | FALSE | Missing/Broken Parts | ||||||||||||||||||
23 | CAM-00031 | 5/20/2017 | Carnival Inspiration | 156 kg of refrigerant gas leaked from an air conditioning system due to a faulty compressor. The system was repaired and put back in service. | Refrigerants | FALSE | refrigerant gas | 156_kg | Refrigerant | ||||||||||||||||
24 | 43513 | 5/22/2017 | HAL Shore Side | On May 22, 2017, Holland America Line and Princess Cruises entered into Settlement Agreements with the State of Alaska for alleged violations of the State’s visible emissions standards. The alleged violations spanned the period 2009 to 2014. | Not Applicable | TRUE | |||||||||||||||||||
25 | 2017-R0637-40-0001 | 5/22/2017 | PCL Ruby Princess | A MBR sample taken that same day from the Ruby Princess, which indicated an ammonia discharge that exceeded the daily maximum. The vessel's onboard sampling results were within allowable parameters, so PCL concluded that the MBRs were not properly processing effluents prior to discharge, which caused ammonia levels to be too high in the overboard samples measured by the ADEC. Following discovery of this issue, PCL cleaned the MBR tanks onboard the Ruby Princess and revised the vessel's desludging frequency requirement based on the vessel's itinerary. PCL received a Notice in response to this self-reported violation on July 13, 2017. | Not Applicable | TRUE | Amonia | Dumping | |||||||||||||||||
26 | CAM-00020 | 5/26/2017 | Carnival Fascination | While checking the Bahamas Annex VI record book for fuel oil and ozone-depleting substances, the EO noted that the Chief Engineer's signature was missing for six entries between March 31, 2017, and May 26, 2017. | Recordkeeping | FALSE | Missing Records | ||||||||||||||||||
27 | CAM-00062 | 6/1/2017 | Carnival Valor | The EO could not locate the original copies of bunker delivery notes for fuel oil (HFO and MGO) bunkered between August 2014 and January 2015 as required by MARPOL Annex VI. Scanned copies of the missing delivery notes are available in the InfoShip system. Flag administration was informed. As a preventive action, all current bunker delivery notes are now being secured in a controlled location. | Recordkeeping | TRUE | Missing Records | ||||||||||||||||||
28 | CAM-00081 | 6/1/2017 | Carnival Fantasy | EGCS SO2/CO2 compliance data was found to be missing from April 22, 2017, through May 1, 2017 due to a computer malfunction. A technician successfully attempted to retrieve the data but was able to reset the computer to restore normal operations. | EGCS | FALSE | Missing Records | ||||||||||||||||||
29 | CAM-00021 | 6/2/2017 | Carnival Ecstasy | The ship discharged food waste and treated black water within 12 NM of Bahamas Archipelagic Baselines on four occasions due to misinterpretation of company policy. Recorded as a water discharge and solid waste discharge. | Voyage Planning | Bahamas waters | TRUE | Sewage, food waste | Dumping | ||||||||||||||||
30 | CAM-00022 | 6/3/2017 | Carnival Conquest | The ship discharged food waste and treated black water within 12 NM of Bahamas Archipelagic Baselines on four occasions due to misinterpretation of company policy. Recorded as a water discharge and solid waste discharge. | Voyage Planning | Bahamas waters | TRUE | sewage | Dumping | ||||||||||||||||
31 | 005_2017-EL.1 | 6/4/2017 | Carnival Elation | Meeting with all Deck and Engine Officer was done and EN000011 discussed with all involved and all Officers understand that discharge of black water and food waste inside Bahamas Archipelagic waters is not permitted. First Officer was aware of requirement but, by mistake, believed that the vessel used BW#14 for grey water and BW#15 for black water and gave an order for flushing of BW#14 once outbound 12 mls from nearest shore. On change of watch at 00:10, OOW, who take over the watch, realized the issue and immediately stopped flushing. | Voyage Planning | Bahamas waters | FALSE | ||||||||||||||||||
32 | 005_2017-EL | 6/4/2017 | Carnival Elation | Approximately 1,270 cubic meters of treated black water and 22 cubic meters of comminuted food waste were discharged inside Bahamian waters in violation of MARPOL and company procedures between June 4, 2017, and June 16, 2017. Discharge was also recorded as a "Other Discharge: Solid Waste." | Voyage Planning | Bahamas waters | TRUE | Black water, food waste | 1270_cubic_meters, 22_cubic_meters | Dumping | |||||||||||||||
33 | CAM-00017 | 6/8/2017 | HAL Nieuw Amsterdam | During ship construction (2009), a drain line from a galley dishwasher was inadvertently connected to an overboard scupper and not to the ship's grey water collection system. This was discovered mid-June 2017 by the ship’s crew. Piping has now been corrected. | Not Applicable | FALSE | Missing/Broken Parts | ||||||||||||||||||
34 | CVL-17-06-0029 Env Open Report #01 2017 | 6/9/2017 | CCL Shore Side | Anonymous caller raised issue regarding Richard Miller, VP CCL. Caller states that he/she has been with the Company for over 17 years as a shipboard employee and that he/she is concerned with Mr. Miller's knowledge of MARPOL, environmental regulations, Corporate procedures, and environmental leadership and stewardship. Caller also stated that this is a concern to other shipboard and shore side team members. | Training | FALSE | |||||||||||||||||||
35 | CAM-00023 | 6/12/2017 | Carnival Ecstasy | 156g of refrigerant gas leaked form an air conditioning system due to the failure of the shaft seal compressor. The system was taken out of service. | Refrigerants | FALSE | refrigerant gas | 156_g | Refrigerant | ||||||||||||||||
36 | CAM-00024 | 6/12/2017 | Carnival Ecstasy | 104 kg of refrigerant gas leaked from a refrigeration system due to a cracked expansion valve fitting. The fitting was replaced and the system put back in service. | Refrigerants | FALSE | refrigerant gas | 104_kg | Refrigerant | ||||||||||||||||
37 | 024_2017-FD | 6/13/2017 | Carnival Freedom | Approximately 467 cubic meters of treated black water/sewage and 6.2 cubic meters of comminuted food waste was discharged inside Bahamian Archipelagic Baseline between June 13, 2017, and June 15, 2017, due to misinterpretation of Bahamas baselines listed in ENV 1001. | Voyage Planning | Bahamas waters | TRUE | sewage, food waste | 467_cubic_meters, 6.2_cubic_meters | Dumping | |||||||||||||||
38 | 005_2017-EL.5 | 6/15/2017 | Carnival Conquest | Comminuted food waste and treated black water from several CCL ships was improperly discharged inside the 12 mile base line of the Bahamas. The cause of these events is not yet clear, although it appears to be associated with the interpretation of procedure ENV1001 (Worldwide Environmental Standards). | Voyage Planning | Bahamas waters | TRUE | sewage, food waste | Dumping | ||||||||||||||||
39 | 005_2017-EL.4 | 6/15/2017 | Carnival Liberty | Comminuted food waste and treated black water from several CCL ships was improperly discharged inside the 12 mile base line of the Bahamas. The cause of these events is not yet clear, although it appears to be associated with the interpretation of procedure ENV1001 (Worldwide Environmental Standards). | Voyage Planning | Bahamas waters | TRUE | sewage, food waste | Dumping | ||||||||||||||||
40 | 005_2017-EL.3 | 6/15/2017 | Carnival Magic | Comminuted food waste and treated black water from several CCL ships was improperly discharged inside the 12 mile base line of the Bahamas. The cause of these events is not yet clear, although it appears to be associated with the interpretation of procedure ENV1001 (Worldwide Environmental Standards). | Voyage Planning | Bahamas waters | TRUE | sewage, food waste | Dumping | ||||||||||||||||
41 | 005_2017-EL.2 | 6/15/2017 | Carnival Vista | Comminuted food waste and treated black water from several CCL ships was improperly discharged inside the 12 mile base line of the Bahamas. The cause of these events is not yet clear, although it appears to be associated with the interpretation of procedure ENV1001 (Worldwide Environmental Standards). | Voyage Planning | Bahamas waters | TRUE | sewage, food waste | Dumping | ||||||||||||||||
42 | CAM-00425 | 6/16/2017 | Seabourn Sojourn | On July 13, 2017, Seabourn self-reported in connection with the Seabourn Sojourn's June 2017 Discharge Monitoring Report that the vessel's BOD levels exceeded the monthly average allowed, and a sample on June 16, 2017, exceeded the daily maximum. To remedy the exceedance, the Company engaged Wartsila, the manufacturer of the Seabourn Sojourn 's sewage treatment system, to conduct a service visit. Seabourn received a Notice in response to this self-reported violation on August 16, 2017. | Not Applicable | TRUE | Missing/Broken Parts | ||||||||||||||||||
43 | CAM-00014 | 6/17/2017 | Costa - CSMART | Costa EO failed CSMART proficiency assessment | Training | FALSE | |||||||||||||||||||
44 | CAM-00025 | 6/20/2017 | Carnival Magic | 350 kg of refrigerant gas leaked from a refrigeration system due to an evaporator failure and loose expansion valves. The evaporator was repaired, the valves were tightened and the system was put back in service. | Refrigerants | FALSE | refrigerant gas | 350_kg | Refrigerant | ||||||||||||||||
45 | CAM-00026 | 6/21/2017 | Carnival Imagination | 1 kg of refrigerant gas leaked from a refrigeration system due to a corroded service valve. The valve was replaced and the system put back in service. | Refrigerants | FALSE | refrigerant gas | 1_kg | Refrigerant | ||||||||||||||||
46 | CAM-00018 | 6/23/2017 | P&O Arcadia | A page was found missing in the ORB onboard Arcadia. CUK stated it was a blank page. | Oil Record Book Recordkeeping | FALSE | Missing Records | ||||||||||||||||||
47 | CAM-00027 | 6/23/2017 | Carnival Conquest | 167 kg of refrigerant gas leaked from an air conditioning system due to Conquest loose evaporator inlet flange. The flange was tightened and the system was put back in service. | Refrigerants | FALSE | refrigerant gas | 167_kg | Refrigerant | ||||||||||||||||
48 | CAM-00029 | 6/23/2017 | Carnival Freedom | 161 kg of refrigerant gas leaked from a provision system due to a failed pipe connection. The pipe was replaced and the system put back in service. | Refrigerants | FALSE | refrigerant gas | 161_kg | Refrigerant | ||||||||||||||||
49 | CAM-00043 | 6/24/2017 | P&O Azura | The ship used HFO for 16 hours while transiting the Icelandic Environmental Protection Zone where Sulphur max is 1.5%, due to a misinterpretation of regulations. Once noted, the EGCS was put online to bring the ship into compliance. | EGCS Voyage Planning | Iceland waters | TRUE | HFO | 16_hours | 960 | EGCS | ||||||||||||||
50 | CAM-00030 | 6/25/2017 | P&O Ventura | During routine maintenance, the calibration certificate of the BCDB oil content monitor (OCM) was noted to have expired. The OCM was checked and found to be within calibration limits. A new certificate was issued. | OCM | FALSE | Missing Records | ||||||||||||||||||
51 | CAM-00032 | 6/25/2017 | PCL Sun Princess | A bypass solenoid and valve were reported missing from the Centrifugal Oily Water Separator (COWS). Investigations found a watch keeping engineer had removed the parts and made a false entry on maintenance into AMOS. The missing parts were replaced and the COWS system was put back in service. There was no overboard bilge water discharge. | OWS/Whitebox Falsification | FALSE | Falsifying Records | ||||||||||||||||||
52 | CAM-00033 | 6/26/2017 | Carnival Liberty | 201 kg of refrigerant gas leaked from a refrigeration system due to a faulty gasket. The gasket was replaced and the system put back in service. | Refrigerants | FALSE | refrigerant gas | 201_kg | Refrigerant | ||||||||||||||||
53 | 08-2017.2 | 6/27/2017 | Costa Deliziosa | The EO onboard the Costa Deliziosa prior to June 27, 2017, believed the requirement to sign the ORB began on July 19, 2017, based on the ship’s interpretation of the relevant ECP section and corresponding HESS procedure. When the relief EO arrived on June 27, 2017, he began signing the ORB, as required. The prior EO was advised of the error and returned to the Costa Deliziosa to sign the ORB pages completed from the date of sentencing through June 27, 2017. | Recordkeeping Oil Record Book | FALSE | Missing Records | ||||||||||||||||||
54 | CAM-00034 | 6/28/2017 | Carnival Dream | 260 kg of refrigerant gas leaked from a refrigeration system due to a faulty pipe. The pipe was repaired and the system was put back in service. | Refrigerants | FALSE | refrigerant gas | 260_kg | Refrigerant | ||||||||||||||||
55 | CAM-00035 | 6/28/2017 | Carnival Imagination | 1.4 kg of refrigerant gas leaked from a provision system due to a faulty valve. The valve was replaced and put back in service. | Refrigerants | FALSE | refrigerant gas | 1.4_kg | Refrigerant | ||||||||||||||||
56 | 004_2017-VE | 6/29/2017 | HAL Veendam | On June 29, 2017, Captain advised HAG shore side of an apparent maintenance mistake on the ship’s Bilge Control Discharge Box (white box). The Captain advised that, during recent maintenance on the ship’s white box, an air pressure regulator/filter was replaced. The replacement was not made in-kind. As a result, the three-way valve in the white box was not operating correctly. The ship tested the calibration of the upstream OCM on the Serep OWS, which was within tolerance for legal discharges. A 4th Engineer noticed the problem and reported up the shipboard chain of command, which was then reported ashore via normal reporting channels. | OWS/Whitebox OCM | FALSE | Missing/Broken Parts | ||||||||||||||||||
57 | CAM-00036 | 6/30/2017 | Carnival Conquest | 264 kg of refrigerant gas leaked from an air conditioning system due to a faulty pipe. The pipe was repaired and the system was put back in service. | Refrigerants | FALSE | refrigerant gas | 264_kg | Refrigerant | ||||||||||||||||
58 | 006_2017-LI | 6/30/2017 | Carnival Liberty | During the EGCS Wash Water Filtration System (WWFS) testing, soot was observed into the water. The system was stopped and the WWFS was inspected. It was discovered that one of the eight filtration bags had ruptured causing the soot to be discharged overboard. | EGCS | FALSE | soot | Dumping | |||||||||||||||||
59 | CAM-00037 | 6/30/2017 | Carnival Sunshine | 208 kg of refrigerant gas leaked from a provision room due to a faulty fitting. The fitting was repaired and put back in service. | Refrigerants | FALSE | refrigerant gas | 208_kg | Refrigerant | ||||||||||||||||
60 | CAM-00038 | 6/30/2017 | HAL Maasdam | During tendering operations in Bar Harbour, USA, a small amount of oil was detected by the bridge near the exhaust of one tender. Further investigation revealed that there was no leak. The discoloring in the water was caused by incomplete combustion from the tender engine. | Lifeboat/Tender | Bar Harbour, U.S. waters | FALSE | ||||||||||||||||||
61 | 001_2017-MJ | 6/30/2017 | PCL Majestic Princess | Majestic Princess made her maiden call to Taiwan on June 30, 2017. On July 5, shore side management was notified of news accounts that appeared to indicate that balloons were released from the ship that could land in the marine environment. After investigation, it was confirmed that the balloons were released shore side and not from the ship. The balloons were arranged by the local PR agency representing PCL. The balloons are reportedly “biodegradable latex” that disintegrates in 2-4 weeks. The release of the balloons required approval of local authorities. We have asked to see proof of the approval. | Not Applicable | Taiwan waters | FALSE | Balloons | Dumping | ||||||||||||||||
62 | CAM-00040 | 7/1/2017 | Carnival Glory | 208 kg leaked from a refrigeration system due to a cracked pipe. The line was repaired and put back in service. | Refrigerants | FALSE | refrigerant gas | 208_kg | Refrigerant | ||||||||||||||||
63 | 007_2017-AT | 7/1/2017 | Costa Atlantica | During an overboard discharge performed through newly installed oil coalescent filtering equipment, the BCDB stopped the overboard discharge due to the OCM showing 18 ppm of oil. The pressure on the delivery side of the OWS was also higher than expected. A test was performed by filling the reading cell with drinking water; however, the oil content still showed 18 ppm of oil. Since previous days, it was also noted that the pressure of the delivery side of the oily water separation circuit of both OWS [coalescent and centrifugal] was higher than expected, causing abnormal noisy working conditions for the pump and consequent line's vibrations. On 18th July, a third-party vendor identified the root cause in a malfunction of the OMD of the BCDB connected to the Westfalia OWS. Therefore, the issue was finally considered as solved. | OCM OWS/Whitebox | FALSE | Missing/Broken Parts | ||||||||||||||||||
64 | 008_2017-NP | 7/2/2017 | PCL Golden Princess | On July 2, 2017, while alongside in Vancouver, Canada, and during the pre-departure motorman checks on board the Golden Princess, it was discovered that the level of the starboard stabilizer header tank was below the level of the sight glass of the lowered header tank on deck 3. Further investigation revealed no sign of an internal leak. The stabilizer housing box venting arrangement was removed and sea water was allowed to enter the vessel and then drained. The quantity of fluid removed was approximately 200 liters of sea water and approximately 5 liters of oil. At no time was an oil sheen observed around the vessel during the evolution. The stabilizer was not in use for a long time. A diver team and Class Representative (Lloyd’s Register) attended in San Diego, CA on July 8, 2017, and completed an external inspection of the starboard side stabilizer. At around 15:00 hrs, the divers reported that there was a dripping of the oil in the starboard side stabilizer housing box. They confirmed that the oil was being contained in the box and not leaving the box into the harbor. The stabilizer housing box venting arrangement was removed and sea water was allow to enter the vessel, the quantity was approximately 200 liters and approximately 2-3 liters of which was oil (oil type: “Mobile SHC aware 68). An oil sheen was not observed around the ship. The Master informed the office and then he reported to the USCG (report number 1183497). A “G” entry in the ORB was made. The quantity of oil discharged into the sea (if any) is unknown. | Not Applicable | Vancouver, Canada port | FALSE | Missing/Broken Parts | |||||||||||||||||
65 | 009_2017-AP | 7/2/2017 | PCL Grand Princess | On July 2, 2017, while Grand Princess was departing Glacier Bay, AK, it was reported that the Oasis port side Jacuzzi was empty. The equipment was switched off and the valves were visually checked. No alarms were activated during the event. Approximately 7.5m3 of water was discharged with bromine content of 4.3ppm and pH 7.4SU. Further investigation revealed that cause of the accidental discharge was due to a failure of the valve automatic timer which is used for pool cleaning purposes. | Not Applicable | Glacier Bay, Alaska waters | FALSE | with bromine content of 4.3ppm and pH 7.4SU | 7.5_cubic_meters | Dumping | |||||||||||||||
66 | CAM-00044 | 7/3/2017 | Carnival Splendor | 267 kg of refrigerant gas leaked from an air conditioning system due to a faulty flange. The flange was repaired and the system was put back in service. | Refrigerants | FALSE | refrigerant gas | 267_kg | Refrigerant | ||||||||||||||||
67 | 010_2017-FA | 7/3/2017 | Carnival Fantasy | During a routine inspection, the EO found several broken seals on the sewage treatment plant. An investigation revealed that 12 seals were broken during monthly routine maintenance but the seals were not replaced. Nine seals were found and replaced; however three, seals could not be found. | Seals or Locks | FALSE | Missing/Broken Parts | ||||||||||||||||||
68 | CAM-00045 | 7/4/2017 | Carnival Ecstasy | 312 kg of refrigerant gas leaked from an air conditioning system due to a faulty pipe. The pipe was repaired and the system was put back in service. | Refrigerants | FALSE | refrigerant gas | 312_kg | Refrigerant | ||||||||||||||||
69 | CAM-00046 | 7/5/2017 | Carnival Splendor | 260 kg of refrigerant gas leaked from various provision systems due to general age-related deterioration. The systems were refilled and was put back in service. | Refrigerants | FALSE | refrigerant gas | 260_kg | Refrigerant | ||||||||||||||||
70 | CAM-00042 | 7/6/2017 | Carnival Elation | On July 6, 2017, the United States Coast Guard issued an inspection report detailing a deficiency relating to MARPOL 1973/78 Annex 1, Regulation 14.7. The ship’s crew were unable to demonstrate the proper operation of the alarm arrangement on the OCM (TD170) fitted to the OWS that is used to indicate when the oil content exceeds 15 parts per million. Additionally, the inspection report requires that the ships IOPPC "Form A" be amended to reflect a maximum throughput of 2.0m3/hour in the event that we can’t demonstrate that the crew are trained and able to show the proper operation of the alarm during the next US port of call. | OCM Training | FALSE | Missing/Broken Parts | ||||||||||||||||||
71 | 011_2017-QM | 7/6/2017 | Cunard Queen Mary 2 | The bowl on the forward OWS failed. The equipment was stopped and isolated. The root cause of the failure is under investigation. | OWS/Whitebox | FALSE | Missing/Broken Parts | ||||||||||||||||||
72 | 05-2017.2 | 7/7/2017 | HAL Koningsdam | Two ships in the Holland America Line fleet, Koningsdam and Noordam, were requested to temporarily assign EO duties to a second engineer (non-watch standing) with the onboard EO. Both Engineers were planned to attend the EO training when they disembarked. The temporary assignment was made on each ship on July 2, 2017, to cover an unplanned gap in EO coverage until a replacement could be sent onboard. This was approved shore side without reference to the applicable requirements of the ECP or the internal procedure, ENV-1008. The ships were directed on July 7, 2017, to reassign the EO duties to the Staff Captain, Chief Engineer, or another senior non-watch standing officer, as required pursuant to the ECP. | Training | FALSE | |||||||||||||||||||
73 | 17-R0720-40-0001 | 7/7/2017 | PCL Island Princess | On July 7, 2017, the Island Princess's smoke emissions exceeded the 20% opacity limit imposed by the applicable Alaska Air Quality Control Regulations while the vessel was moored in Ketchikan. Princess Cruise Lines actively cooperated and conferred with the ADEC during the weeks following this incident and concluded that the exceedance was caused by the vessel's burning marine oil gas while the EGCS was not properly running. There were no upsets with the combustion sources. Princess Cruise Lines received a Notice related to this occurrence on December 1, 2017. | Not Applicable | Ketchikan, Alaska port | TRUE | EGCS | |||||||||||||||||
74 | 012_2017-OR | 7/8/2017 | P&O Oriana | While alongside in Palermo, Italy, an unknown quantity of chlorinated recreational pool water was discharged due to a faulty pump valve. | Not Applicable | Palermo, Italy port | FALSE | chlorinated recreational pool water | Dumping | ||||||||||||||||
75 | 002_2017-TP | 7/8/2017 | PCL Star Princess | Two ships in the Holland America Line fleet, Koningsdam and Noordam, were requested to temporarily assign EO duties to a second engineer (non-watch standing) with the onboard EO. Both Engineers were planned to attend the EO training when they disembarked. The temporary assignment was made on each ship on July 2, 2017, to cover an unplanned gap in EO coverage until a replacement could be sent onboard. This was approved shore side without reference to the applicable requirements of the ECP or the internal procedure, ENV-1008. The ships were directed on July 7, 2017, to reassign the EO duties to the Staff Captain, Chief Engineer, or another senior non-watch standing officer, as required pursuant to the ECP. | Not Applicable | FALSE | |||||||||||||||||||
76 | CAM-00048 | 7/9/2017 | Carnival Dream | 260 kg [sic] leaked from a provision system due to a cracked pipe. The pipe was repaired and was put back in service. | Refrigerants | FALSE | refrigerant gas | 260_kg | Refrigerant | ||||||||||||||||
77 | CAM-00049 | 7/9/2017 | PCL Caribbean Princess | During tendering in South Queensferry, Scotland, a tender engine in operation had a defective fuel pump resulting in a minor oil sheen on the water. The engine was stopped, the tender was recovered, and the fault was repaired. | Lifeboat/Tender | South Queensferry, Scotland port | FALSE | oil sheen | minor | Dumping | |||||||||||||||
78 | CAM-00050 | 7/10/2017 | HAL Zuiderdam | A hydraulic oil leak was found on the forward davit arm of a lifeboat. The lifeboat has been taken out of service pending the investigation and repair. | Lifeboat/Tender | FALSE | oil | ||||||||||||||||||
79 | CAM-00051 | 7/10/2017 | Carnival Magic | 413 kg of refrigerant gas leaked from a refrigeration system due to a crack in the main line. The pipe was repaired and the system put back in service. | Refrigerants | FALSE | refrigerant gas | 413_kg | Refrigerant | ||||||||||||||||
80 | CAM-00052 | 7/11/2017 | Carnival Fantasy | 307 kg of refrigerant gas leaked from an air conditioning system due to a corroded pipe. The pipe was repaired and the system put back in service. | Refrigerants | FALSE | refrigerant gas | 307_kg | Refrigerant | ||||||||||||||||
81 | CAM-00053 | 7/13/2017 | Carnival Paradise | While underway, after exiting US Vessel General Permit waters but within the North America ECA area, the ship burned HFO for approx. 40 minutes until the changeover to MGO was completed. | Voyage Planning | U.S. waters | TRUE | HFO | 40_minutes | 40 | EGCS | ||||||||||||||
82 | 025_2017-PR | 7/13/2017 | Carnival Pride | While anchored at Half Moon Cay (within the Bahamas Archipelagic Baseline), a plastic bin containing a plastic bag and non- comminuted food waste fell into the sea due to it being not properly secured to a pallet. Incident occurred when one local tender was transferring back to ship the food waste generated on the island. Half Moon Cay does not have a waste facility and hence all food waste that is generated on the island by the ships guest are brought back on board to be disposed of by the ship. The plastic bin, waste bag, and some food waste was recovered but approximately 15 pounds of food waste could not be recovered. | Not Applicable | Half Moon Cay, Bahamas port | TRUE | food waste | 15_pounds | Dumping | |||||||||||||||
83 | CAM-00082 | 7/13/2017 | Carnival Splendor | 260 kg of non-ODS refrigerant gas leaked from an air conditioning system due to a failure of a discharge valve. The valve was replaced and the system put back in service. | Refrigerants | FALSE | non-ODS refrigerant gas | 260_kg | Refrigerant | ||||||||||||||||
84 | 003_2017-AD | 7/14/2017 | P&O Adonia | While alongside in Southampton, UK, discharging sludge, the hose connected to the tanker failed causing approx. 20 liters of oil sludge to spill onto the ship and into the harbor. Absorbent booms, pads, and other materials were used to clean up the oil and prevent the oil from spreading. The Port Authority was notified and the waste vendor assisted with the cleanup. | Not Applicable | Southampton, UK port | TRUE | oil sludge | 20_liters | Dumping | |||||||||||||||
85 | 019_2017-SL | 7/15/2017 | Carnival Splendor | Treated black water was potentially discharged inside Bahamas baseline due to accidentally opening the overboard discharge valve. The valve was closed within 10 minutes. Compliance verification was done with the fleet in June 2017 regarding the proper understanding of the Bahamian baseline and associated discharge restrictions. This incident was caused by a separate human error and not a fundamental misunderstanding of the baseline restrictions. | Voyage Planning | Bahamas waters | TRUE | sewage | Dumping | ||||||||||||||||
86 | CAM-00054 | 7/16/2017 | Carnival Valor | 260 kg of refrigerant gas leaked from a refrigeration system due to ship vibrations. The system was repaired and put back in service. | Refrigerants | FALSE | refrigerant gas | 260_kg | Refrigerant | ||||||||||||||||
87 | 020_2017-FS | 7/17/2017 | Carnival Fascination | During the review of the bilge system, a discrepancy was found between the actual and the approved design layout of the system. An actual design layout drawing will be completed. | Not Applicable | FALSE | Missing/Broken Parts | ||||||||||||||||||
88 | CAM-00055 | 7/17/2017 | Carnival Glory | A missing seal was found on the vacuum line of the sewage treatment plant. An investigation revealed the seal was accidently broken but not noticed by engine personnel. The seal was replaced and the system put back in service. | Seals or Locks | FALSE | Missing/Broken Parts | ||||||||||||||||||
89 | CAM-00056 | 7/17/2017 | PCL Star Princess | While underway, recreational water was discharged overboard due to electrical failure. | Not Applicable | FALSE | recreational water | Dumping | |||||||||||||||||
90 | 014_2017-VI | 7/18/2017 | Carnival Victory | During maintenance checks, it was noted that the ship was missing original hardcopy fuel bunker delivery notes between July 2014 and January 2017. Ship has electronic copies of the bunker notes contained in InfoShip. Search on board to find missing folder has not recovered the original documents. | Recordkeeping | FALSE | Missing Records | ||||||||||||||||||
91 | 028_2017-NA | 7/18/2017 | HAL Nieuw Amsterdam | While alongside in Skagway, Alaska, a full blackout occurred during an emergency shutdown system test. Incorrect procedural instructions were found in the job description of AMOS. Power was recovered quickly. | Not Applicable | Skagway, Alaska port | FALSE | Missing/Broken Parts | |||||||||||||||||
92 | CAM-00019 | 7/19/2017 | PCL - Various Vessels | 2 PCL ships that likely won’t meet the July 19, 2017, deadline to have accurate and class approved drawings onboard. | Not Applicable | FALSE | Missing Records | ||||||||||||||||||
93 | 021_2017-MA | 7/19/2017 | HAL Maasdam | The ship sailed in an air emission control area for 45 minutes running an engine on HFO due to the EGCS being accidentally stopped. Three DGs running during the approach and arrival into Charlottetown. Two DGs were running on MGO (DG1 and DG3) and one generator was running on HFO (DG5) with EGCS in operation. Although not required, in order to keep the system running and flushing, the EGCS on DG 3 was also running. Shortly before ‘red manning’ status for arrival, the scrubber of DG 3 was shut down to enable cleaning of the sea chest. Due to an internal communication error, the scrubber of DG5 (on HFO) was accidentally shut down as well. Between 07:44 and 08:26, DG 5 was running on HFO without the scrubber in operation. DG1 and DG3 were in operation on MGO at all times. As soon as it was identified that the EGCS for DG5 had been shut down (DG5 still on HFO) the ship changed over from DG5 to DG4. DG4 was already operating on MGO. As soon as the DG4 was on the board, DG5 was stopped. That all happened while maneuvering on arrival in Charlottetown. | EGCS Voyage Planning | Charlottetown, Canada waters | TRUE | HFO | 45_minutes | EGCS | |||||||||||||||
94 | 016_2017-EC | 7/21/2017 | Carnival Ecstasy | The ship sailed in an air emission control area for nearly two hours with an engine running on HFO. The EGCS had automatically shut down due to water in the sensor. The Engineer On Watch acknowledged the alarm, but did not realize the significance of the issue and did not investigate. Subsequently, email was received from MST2 Marcus Thompson, USCG Sector Charleston Prevention, asking for relevant info about the issue, so he was replied back with all detailed info about the same. Thereafter, on July 22, 2017, around 12:30 pm, USCG MST1 Dan Mitchell, boarded the vessel and enquired about the same. The Master, Chief, and EO provided the same information. Mr Mitchell gave a Port state control inspection report Form A and Form B, indicating the following: Action taken: 16 (a,c). The report requests an audit from Recognized Organization ( Lloyd’s ) for this issue with given time frame of 14 days from today. | EGCS Voyage Planning | TRUE | HFO | 2_hours | 120 | EGCS | |||||||||||||||
95 | 43633 | 7/22/2017 | Costa Luminosa | On July 22, 2017, the OLCM for Costa Group (Costa Crociere and AIDA Cruises), Alessandro Bertorello, was informed by his Environmental Compliance Manager, Alessandro Pugliaro, that there may be an issue with recent training records on the Costa Luminosa. When Alessandro Pugliaro embarked the Costa Luminosa on July 22, 2017, for a one week visit he was informed by the disembarking EO (EO), Giulia Facelli, and her replacement, Stefano Incao, that records of a training session that allegedly took place on June 6, 2017 may have been falsified. The training in question was allegedly held by the EO onboard at the time, Marcio Goncalves. The training session records showed several pages of signatures confirming attendance. Since notification of this issue, multiple interviews have been conducted with those onboard, who have confirmed that they never took part in the alleged training and that the signatures are not theirs. | Training Recordkeeping Falsification | FALSE | Falsifying Records | ||||||||||||||||||
96 | 018_2017-SP 021_2017-SP 07-2017 | 7/22/2017 | Carnival Spirit | On July 22, 2017, it was brought to the attention of the shore side environmental operations team via email from the EO that the Carnival Spirit had not been recording the periodic maintenance of the OCMs in the ORB since April 19, 2017. Periodic maintenance of the OCMs is recorded and visible in PMS, but not in the ORB. All PMS Entries are available in infoship | Oil Record Book Recordkeeping | FALSE | Missing Records | ||||||||||||||||||
97 | 027_2017-VE | 7/22/2017 | HAL Veendam | The critical control units of the OCMs and waste water treatment plants are displaying error messages and need repair or replacement. There are currently no spare units on the ship. During routine, reoccurring maintenance, the spare PLC was inspected and found to be malfunctioning (60 monthly, AMOS job #TESTPLC001). The PLC currently installed is operational and functioning correctly. | OCM | FALSE | Missing/Broken Parts | ||||||||||||||||||
98 | 015_2017-VITA | 7/23/2017 | AIDAvita | While underway, the flow pressure rate of the OWS was low due to the outlet piping being too small in diameter. The Chief Engineer of AIDAvita reported that the newly installed Westfalia oil filtering equipment worked at a lower flow rate (2m3/h) than the one the system should work at (5m3/h) when discharging overboard. Flow rate in recirculation mode was not affected; therefore, the issue was attributed to the overboard piping diameter. No pollution or MARPOL violation involved | OWS/Whitebox | FALSE | Missing/Broken Parts | ||||||||||||||||||
99 | 017_2017-VS | 7/23/2017 | Carnival Vista | Carnival Vista while returning to Miami sailing through Bahamas Channel accidently discharged Comminuted Food Waste and Treated Black Water (AWPS) inside Bahamas Base Line. Approximate quantity of the Food Waste discharge was 4.0 m3 and Black Water from AWPS was 100 M3. Crew was aware of baseline issue, properly planned and briefed multiple times; human error by watch officer in authorizing discharge. When the Officer on Watch realized the mistake, he immediately stopped all discharge operations and self-reported. Compliance verification was done with the fleet in June regarding the proper understanding of the Bahamian baseline and associated discharge restrictions. This incident was caused by a separate human error and not a fundamental misunderstanding of the baseline restrictions. | Voyage Planning | Bahamas waters | TRUE | sewage, food waste | 100_cubic_meters, 4_cubic_meters | Dumping | |||||||||||||||
100 | 032_2017-MI | 7/23/2017 | Carnival Miracle | During a review of the ORB, it was noted that entries for periodic maintenance were not recorded. A meeting was held to discuss and clarify the requirements with the Engineer Officers. Entries for performed maintenance to bilge equipment were not recorded in ORB as per company procedures and ECP requirements. PMS was performed and recorded in InfoShip; however, additional entries in the ORB as required by the ECP were not made. | Oil Record Book Recordkeeping | FALSE | Missing Records |