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Motor

Design Review

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CAD

Bates Propellant Grains

Nozzle Carrier

Forward Closure

Graphite Nozzle in

Phenolic Insulator

Boat Tail

Phenolic Liner

Finocyl Grain

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CAD - Nozzle Carrier

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Design - Nozzle Carrier

Nozzle Carrier

Aluminum replaced with Phenolic around Graphite Nozzle

  • Lower Average Density - Overall Mass Savings (1.5 lb)
  • Insulates Aluminum from Thermal Stresses
  • Protects Aluminum from Erosion - Aluminum is Reusable

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CAD - Case

79”

Bolted Aluminum Case with 5/16” Bolt Holes (attach to forward closure/nozzle carrier)

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Bill of Materials - Reusable

Name

Material

Mass

Cost

Motor Case

Aluminum 6061-T6

34.5 lb

$375

Nozzle Carrier

Aluminum

4.38 lb

$85

Nozzle

Graphite

1.92 lb

$30

Boattail

Aluminum

3.29 lb

$95

Forward Closure

Aluminum

2.41 lb

$50

Bolts

Alloy steel

0.6 lb

$15

Subtotal

47.1 lb

$650

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Bill of Materials - Consumables

Name

Material

Mass

Cost

Liner

CE Phenolic

6.39 lb

$550

Nozzle Insulator

LE Phenolic

0.93 lb

$50

Propellant

APCP (Cherry Limeade)

72.6 lb

$875

Subtotal

79.9 lb

$1475

Total

127 lb

$2125

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Summary of Changes from ‘17/’18

  • Improved Propellent - better density, ISP, and burn characteristics
  • Grain Geometry - Aft finocyl for high-force initial kick-off and lowered port mass flux
  • Lighter and more thermally insulating nozzle carrier
  • Bolt size reduction for cleaner assembly & reduced drag
  • Revised Liner - Better thermal insulation, no spiral ‘weak points’, tighter tolerances

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Design

New Propellant Formulation - Cherry Limeade

Changes from OW:

  • Higher Solids Loading (82.5%)
  • Removal of Burn Rate Catalyst
  • Change from Trimodal to Bimodal AP

Results:

  • Density increased 7% (0.057 -> 0.061 lb/in³)
  • Viscosity increased slightly - still pourable
    • Solids loading could increase to 83-84% in the future

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Design

Formulation Specifics

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Analysis

Characterization Fire - 6 motors with different KN tested

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Analysis

Characterization Results

ISP ~= 200 s (without a divergent section)

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Design

Grain Geometry

Grain length increased - number of grains decreased�Aft grain replaced with a finocyl (demonstrated in January 2018)�Resultant burn profile split into two phases:

  • More force early in the burn - easier to get off the launch pad while rocket is still heavy
  • Gentler sustained second phase - reduced loads on the case when weakened by heat soak, better expansion ratio at lower atmospheric pressures

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Analysis

Burnsim Data - Grain Geometry

Propellent Mass - 72 lb

Burn Time - 8.5 s

Impulse - 73000 Ns (P-8600)

ISP - 233 s

Max Pressure - 880 psi

Max Thrust - 2950 Lbf

Pressure Thrust

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Analysis

Static Analysis - Case Stress

Max Stress in Case: 96 MPa

Below Yield Stress of Al-6061-T6 up to 475 K - Use phenolic liner to insulate case

Potential to reduce wall thickness from 1/4” to 3/16”

  • 9 lbs of predicted mass savings
  • Stresses would increase by 1.33x (as σ ∝ 1/t)
  • Requires thermal modelling to verify case temperature (data collection and simulation)

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Analysis

Static Analysis - Notes on FEA Sim

  • The model considers the loads on the aluminum case rigidly bonded to the forward closure and nozzle carrier (loads on connecting bolts analyzed elsewhere)
  • 1400 psi pressure (~1.75x the expected maximum pressure) applied to inside of case
  • A 2000 lbf load applied vertically downwards at top of case to model weight of mission package (~40 lb) at 25G and aerodynamic drag force of 950 lbf
    • Effect of this found to be negligible compared to pressure loads

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Analysis

Bolts & Fasteners

Bolts changed 3/8” -> 5/16”�Assuming max shear stress of 2.28 ✕104 psi with a factor of safety of 1.8x

  • Allows countersinks to be flush with�the wall of the case
  • Mass Decrease (6 oz)

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Analysis

Propellent Mechanical Properties

Instron Test samples of CL to find elastic modulus, poisson ratio, and other mechanical properties

Use these to perform load analysis on propellant grains to ensure they won’t crack during flight under high acceleration

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Manufacturing - Hardware

  • Axisymmetric parts (Nozzle, Carrier, Closures) machined on lathe
  • Radial Holes drilled on Mill w/ Indexing Head
  • Phenolic: waterjet from sheet, glued into round, then machined

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Manufacturing - Propellent

  • Ingredients mixed in a 30 quart mixer
  • Propellent placed under vacuum to remove bubbles before casting
  • Cast into grain-shaped casting tubes around taped mandrels
  • Grains cured overnight
  • Cured grains cut to length, ends are sanded

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Manufacturing - Mixing Procedure

1. Add HTPB, IDP, and Castor Oil

2. Mix for 5 minutes

3. Add AL

4. Hand mix until wetted out, machine mix for 10 minutes

5. Add PDMS and Triton X-100

6. Mix for 30 minutes

7. Vacuum for 45 minutes

8. Repeat until all 200 AP is in:

a. Add a third of the original mass of AP

b. Mix for 1 minute

c. Scrape down

d. Mix for 10 minutes

9. Add the 90 AP

10. Mix for 1 minute

11. Scrape down

12. Mix for 45 minutes

13. Add curative

14. Mix for 20 minutes

15. Vacuum for 45 minutes

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Manufacturing - Finocyl

Procedural Changes

Finocyl Grain uses modified process:

  1. Fabricate Core Mandrel - Use foam wire cutter to cut profile of port out of foam
  2. Waterjet End Caps - Matches port geometry
  3. Cast Grain - uses standard process
  4. De-mold grain - Dissolve core mandrel with acetone

Process demonstrated in IAP/Spring 2018

Improvements:

  • Core Stiffness
  • Foam Cutter Reliability
  • Removal of Splice Point

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Manufacturing - Propellent

Pneumatic Sieve Shaker

  • Uses pneumatic vibrator to shake AP 200μm and smaller through filter

18”

23”

Pneumatic vibrator

Material

Cost

$7.52

$22.09

~$65.12

$52.32

$38.8

Cover between bucket and bowl

N/A

5 gal Bucket

$3.25

Rubber shock absorbers

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Manufacturing - Motor Assembly

  • Nozzle assembly:
    • The three-piece nozzle assembly is fit-checked, then each sealing surface is coated in RTV. The pieces are then assembled
  • Grains glued into liner with grain spacer O-rings
    • 5-minute epoxy used for grain-bonding process
  • Liner placed into case
  • Other hardware bolted on

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Testing

What do we need to do to make sure we can fly the rocket?

  • Propellant Characterization - Completed
  • Hydrostatic Testing - Up to 1400 psi
  • P Motor Static Fire - Scheduled by End of Semester
  • Propellent Mechanical Testing - January

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Risk Matrix

Risk

20%

10%

5%

3

4

1%

2

0.1%

5

8, 9

1, 7

6

1

2

3

4

5

Subsystem

Impact

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Risks and Mitigations for Flight

ID

Risk

Impact

Likelihood

Difficulty of fix

Mitigation

RE

1

O-ring failure

4

1

1

Ensure proper groove dimensions.

Israel Bonilla

2

Nozzle cracks

3

2

2

Increase the size of the graphite nozzle.

Alexander Salisbury

3

Aluminum carrier erodes

2

3

2

Increase the size of the phenolic carrier.

Israel Bonilla

4

Liner splice failure

5

3

3

Follow SOP for liner splicing. Use CE phenolic.

Jamie Abel

5

Bolt failure

2

1

1

Correctly perform bolt calculations.

Joshua White

6

Case failure

5

1

1

Use a ¼” wall thickness case.

Joshua White

7

Closure failure

4

1

2

Insulate the closure with a phenolic disc.

Israel Bonilla

8

Ignition failure

3

1

1

Day-before/Day-of functionality checks.

Andrew Reilley

9

Propellant cracks

3

1

3

Properly cure the propellant.

Julia Gaubatz

Impacts, likelihoods, and difficulties are listed on a scale from 1 (very low) to 5 (extreme)

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Open Issues

  • Liner Splicing
  • Thermal Modelling Capability
  • Lab Space Change

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Schedule to Completion

Needed Procedures

Intended Deadline

Propellent Characterization

Completed 10/27/18

Motor Design Review

In Progress - 11/20/18

Manufacture 6” Hardware

11/30/18

Mix 6” Grains

11/30/18

P Motor Assembly

12/1/18

P Motor Static Fire

12/8/18

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Questions?